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Stories of Leadership, Lean, and Learning

From Tool Boxes to Tool Stations

In 2011, I was asked to facilitate a changeover reduction Kaizen event at a ceiling tile plant in Florida. Most changeover reduction events have a goal of reducing time by 50%, while maintaining or improving quality and safety. In this case, the team was asked to reduce changeover time by 90%. This would be a challenge for the team and my ability to facilitate them to a solution.

The area chosen was the edge finishing line. The line cut and painted edges on the ceiling tiles before sending them on to the packaging line. Using a panel saw called an equalizer, tiles were cut to a rough size. Four tenoners cut and painted the edges of the tiles to achieve precise outer dimensions and edge finish. The tiles were designed to fit snugly into ceiling grid. A portion of the tile hung below the surface of the grid, creating a three-dimensional visual.

The tenoners had dozens of adjustment points, requiring wrenches and other tools to meet the strict dimensional tolerances. All technicians had their own personal toolbox, which they stored far away from the line. When it was time to adjust or set up the tenoners, they gathered their personal tools and brought them over to the tenoner they were adjusting at the moment.

After training the team in Lean principles and Single Minute Exchange of Die (a changeover reduction approach) we watched a changeover conducted by the crew on shift. What we saw was a tremendous amount of movement by the technicians conducting the changeover. Most of the movement was due to each technician gathering and moving tools back and forth between the line and their personal toolboxes which were stored thirty yards from the tenoners.

The changeover took ninety minutes. Our goal was to achieve a consistent nine-minute changeover. I wasn’t sure it was possible, but there appeared to be a tremendous amount of opportunity, especially in the area of tool use and placement.

After brainstorming overall improvement ideas, I facilitated the team to focus on ways to eliminate the huge amount of movement we observed. The plant was built in the 1940’s. Most technician habits developed over many decades of production. I wasn’t sure people would be willing to change their approach and give up their personal toolboxes.

They weren’t willing to, but it didn’t matter. The team realized their toolboxes should be set up to do unscheduled repairs and adjustments. Placing tools right at the place they were needed, would save a huge amount of time during changeover.

We identified three tools used to set the tenoner saws and edge paint sprayers precisely. They were needed in eight separate locations. Were we willing to replicate those three tools eight times?

If we wanted to cut the time by ninety percent, we had to be willing to try extreme measures. I went to the hardware store and bought eight sets of tools. The team mounted them exactly where they were needed for the changeover.

In addition to the tools, we created visuals to show the steps and installed a large digital clock on a post. It displayed the changeover elapsed time. We tested our new procedure with all of the improvements and were able to complete the changeover in fifteen minutes by the end of the Kaizen event.

Although we didn’t meet our goal, changeover time was reduced by 83%. The team felt like they had won and the plant reaped the benefits of a safer and quicker changeover for many years thereafter.